Flight 2 departed Sea-Tac at just after 8:00 AM. Its intended itinerary would have taken the aircraft to Portland, Chicago, and New York City. The takeoff was uneventful until the first officer retracted the wing flaps; the aircraft suddenly began to buffet violently and also began a roll to the left. The captain believed that an asymmetric wing flap condition--when one set of flaps retract, but the other set of flaps remain extended--had developed and made numerous attempts to control the aircraft, but to no avail. Believing the aircraft unairworthy, he considered returning to Sea-Tac and diverting to McChord Air Force Base, but the buffeting worsened and the Stratocruiser began to lose altitude. They decided their best chance was to ditch in the relatively shallow and calm waters of Puget Sound. The first officer's Mayday transmission relaying the intention to ditch was heard by the captain of a Coast Guard vessel and the pilot of an Air Force amphibious Grumman Albatross aircraft, both of whom readied their vessels to assist the stricken aircraft. The captain brought the aircraft down smoothly. Although it took on water quickly, the passenger cabin remained in one piece, and all of those on board were able to depart safely, most using their seat cushions as makeshift flotation devices. The Air Force Grumman landed in the water near the ditching site ten minutes after the ditching and launched a number of inflatable liferafts, but not all passengers and crew were able to reach them; many remained in the freezing waters of Puget Sound hanging onto their seat cushions until they were rescued less than thirty minutes later by the Coast Guard vessel. Four passengers, including a six-year-old boy and his mother and one male flight attendant, were not recovered and were thought to have succumbed to hypothermia. The Stratocruiser sank 15 minutes after the ditching in approximately of water.
Investigation
Investigators with the Civil Aeronautics Board determined that the underlying cause of the accident was a single error made by the flight engineer. Stratocruiser engines were cooled by opening panels called "cowl flaps" or "engine cooling flaps" which circled the rear part of the engine and allowed heat to dissipate when open. The open cowl flaps could also disrupt the flow of air over the wings and it was therefore necessary to close them during critical phases of flight such as takeoff when maximum lift was needed. When the captain during his pre-takeoff checklist called, "Cowl flaps set for takeoff", the flight engineer replied "Set for takeoff", but had not actually closed them. When the aircraft took off and the wing flaps were retracted, the loss of lift caused by the open engine cowl flaps caused the aircraft wings to partially stall. Tests performed by CAB investigators showed that a Stratocruiser that took off with all cowl flaps open would respond very similarly to a Stratocruiser with one engine shut down and could be turned and flown for some time before becoming too unstable to remain in the air. However, the captain was convinced that the problem had been caused by asymmetric wing flaps, a situation that would make all but the slightest turn dangerous, and decided to ditch based on that analysis. The CAB found that the captain had incorrectly identified the cause of the aircraft's control and stability problems, but that it would have been extremely difficult if not impossible for him to have correctly identified the problem given the information he had, the nature of the emergency he was faced with, and the time in which he had to make the decision as to whether to ditch or to attempt a landing at McChord AFB or back at Sea-Tac. The accident flight is known in some references as Northwest Airlines Flight 2; it actually flew under the Northwest Orient Airlines name. Northwest advertised itself as Northwest Orient Airlines from the late 1940s to its merger with Republic Airlines in 1986; the registered corporate name remained "Northwest Airlines", thus the CAB report's designation is correct.